Denker's Mini Mill PAGE


Home Built Mini Mill Information

My mill is a combination of purchased mini mill assemblies and other purchased and fabricated parts. The head assembly (R8) and column are standard mini mill with a purchased compound mill table mounted on a 1/2" thick steel base. Everything is greatly modified. The column does not rotate on the base like the standard machine, but is held vertical by 0.25" thick supports and a 4" webbed iron angle plate. Instead of the standard head support spring or gas support system, I am using a counterbalance. (far better) I went with a different table because I wanted something a bit heavier and 0.100" per rev. dials. I used a standard 5" x 8" PHASE II table and modified it. For the most part it came out very well but I would recommend using a large U-beam for a base instead of a flat plate. My plate required extra supports.

Mill

 (Updated picture as of Oct. 2020)

 

Modification Contents:

 Compound Table

 Counterweight

 Low Speed Addition

 Table Power Feed

 Z-Axis Control (Changed)

 Other Additions & Changes (Changed)

Home


 

Compound Table

The mill table I bought was a little on the ruff side. I paid about $70 for it and it showed. The acme screws had between 0.010" and 0.015" of backlash and the handles were too small. It came with the X-axis handle on the left so I switched it to the right side. To remove some of the backlash, I added thrust bearings and made new longer acme screw shafts to accommodate the extra length of the thrust bearing housing. (Also added length for a power feed unit) As long as I was doing that, I made new acme nut brackets too. Now the backlash is under 0.005". It would be better if I used better acme nuts or bought a 1/2-10 acme tap and made my own. I also had to add X and Y-axis lock handles (this table did not come with them) and added inch scales. Finally I replaced the 2.5" handles with 3.5" brass ones to get an easier feel. Overall this was quite a bit of work for a heavier duty table. Was it worth it? - I think so. To get 0.100" per rev. feed, there are not many low priced options out there. For a heavy duty table it is well designed, milling chips do not get anywhere they shouldn't and is just about the right size. After the improvements, I would say it has been very good.

Back to top

Home


 

Counterweight

From what I have read and seen on the Internet, the mill head support systems used on the standard mini mills are not very good. I decided to go with a counterweight system instead. I mounted a 4" pulley on top of the column and a 10" THOMSON linear bearing bar (surplus) on the back for the weights. I connected the head to the weights with a plastic covered steel cable. The motor controller box had to be mounted on the left side of the column. It works great but adds major weight to the machine.

Back to top

Home


 

Low Speed Addition

This is a big project that required a large amount of engineering and just as much machining. It gives the machine a 0 to 700 RPM speed range with 1.5 times the output torque. It also bypasses the internal plastic gears. The motor is mounted on a position plate so it can be moved forward or back. To engage the low speed range, I move the motor to the rear position where it engages a different gear. This system reverses the spindle direction so a reverse switch must also be added. This is not a easy addition but it sure is worth it. I can now use bigger drills and mills and with the reverse switch I can use it for tapping without a big tap head. The housing is made of 1/2" thick aluminum plates layered 3 high and bolted and pinned together. It uses the same timing belt system as the low speed addition of my mini lathe but with a gear instead of the V-belt. I changed the gear on the motor from a 16-tooth to a 15-tooth so the higher speeds are now 0 to 1040 RPM and 0 to 2380 RPM.

milllowspeed

This housing also has a spring-loaded spindle lock pin. (Updated Oct 2020)

Millgears2.JPG

Back to top

Home


 

Table Power Feed

This is not an easy project and required considerable engineering. The housing is a 3" x 3" x 0.125" thick square aluminum tube that encloses the switches, relays, gearing and bearings needed for the drive. I'm using a 30VDC motor that draws about 1 amp and has a motor overload protection circuit set at about 1.5 amps. It also has stop switches for adjustable position stops located behind the compound table. There is an engagement lever to engage the X-axis acme screw because a worm gear is used in the design and the X-axis cannot be moved by hand with the power feed engaged. The maximum feed rate of this system is about 8" per minute. A separate box located behind the mill houses a power transformer, circuit breaker for the unit, SCR controller board and Hi/Lo feed speed switch.

newxdrive.JPG

(Updated Jan 2021)

Back to top

Home


 

Z-Axis Control:

I have found z-axis head control can be a little tricky for some operations. Because the hand and fine feed controls use a gear and rack, which has a bit of slop, operations like drilling out large holes, boring and vertical milling can be a problem. To make this easier I added a z-axis screw. Others have done this and I found it helpful too. For normal operation, I remove the two bolts from the screw head bracket and rotate it 180° to the back. (Shown just under the head locking lever) I am using a 1/2"-20 threaded rod so each turn moves the head 0.050". The purchased rod I used is not dimensionally accurate and is off by about 0.040" in 10 inches. I would have to make my own screw if this was not good enough in the future. With this now in place, I removed the old fine feed system.

Now I have added a Z-Drive motor with its gearbox and a control box. The motor was salvaged from an old paper shredder and the control box uses a variable transformer for speed control. The gear box is hinged so it can be disconnected from the lead screw. I also added Top and Bottom limit switches with the bottom one movable. This works great when using a Boring Bar Head.

Zdrive.JPG Zcontrol.JPG

Back to top

Home


 

Other Mill Additions & Changes:

 It is an absolute must to have a Z-axis indicator. This one uses an addition to the mill stop bracket to engage a 1" travel indicator mounted to the mill head. I have a 1" and 2" spacer that can be added when setting it up to get longer movements. (up to 4" total)

 In the above picture you can also see an added column chip guard. It is a thin rubber mat cut to about 5.5" x 12" with weight added on the bottom and mounted to the mill head. It's cut just long enough to protect the wear surfaces. As the head moves down, it folds in place.

 Another addition that is very nice at times is a X and Y-axis indicator. This takes the guesswork out of the backlash of the table. For less wear on the indicators, I only mount them when needed. (This is the Y-axis one.) I have not added any DRO's because the good ones cost so much and I haven't really needed them. (Maybe in the future?)

 

 I have a small air compressor in my shop and have air blow off brackets and nozzle that can be mounted on the mill. I have also added a flexible air nozzle on the left side of the mill.

 Millair.JPG

 

 I have redone the lighting on the mill head using LEDs. This is a much cleaner and brighter system. I am using 3 120VAC LED modules that are hooked into the mill control box for power. I replaced the green light in front with a switch so I can turn these off when needed. (when using a laser center)

Millled.JPG Millleds.JPG

 

 This is a chip containment box I have mounted on the compound table. It is easily removed with 6 thumbnuts when milling large parts or for long parts, ether side can be replaced with a shorter version. With it and the mills stock shield, I can contain over 95% of the metal chips in the box. It sure makes cleanup easier!

 

 This is my drawbar wrench and mallet. It was made from an old broken 3/8" ratcheting socket wrench and an 18mm socket. Also added was a 1 3/8" dia. plastic mallet end.

Back to top

Home


All pictures and content Copyright © 2007, 2008, 2009, 2020, 2021 David Denker. All Rights Reserved.

Last Revised: Feb. 2021